Flint & Walling has a selection of submersible pumps and jet pumps designed with robust components to deliver superior performance across a range of applications.
Flint & Walling offers a selection of reliable water pumps and systems designed to help you maintain lush lawns and vibrant gardens. Browse our catalog to find the product that suits your needs.
From pressure boosting to maintaining constant pressure or regulating pressure, our range of water pressure booster pumps offer tailored solutions to tackle any challenge effectively.
Our tailored products ensure livestock comfort by providing reliable water supply solutions specifically designed for use in poultry houses and livestock environments
A car wash cannot perform efficiently with low water pressure. These products are a great solution for these applications where you need high and consistent pressure.
Flint & Walling has a large selection of water pumps suitable for residential, commercial, and industrial applications. Engineered using high-quality materials, our products provide value and efficiency.
While pumps form the core of our operations, achieving their peak performance often necessitates the integration of supplementary controls or frequency drives.
When raising livestock, it is crucial to keep the animals cool with a steady water supply. We have specially designed these products for use in poultry houses and livestock areas.
Centrifugal applications include booster service, water circulation, liquid transfer, cooling systems, jockey pump service and general service in farm, commercial and industrial applications.
Having a bit of trouble with your product? We’re here to help. Here are some common topics we are asked about. Or need more individualized assistance? Reach out to our Groundwater Support Team!
Groundwater Support Phone: 1-800-628-2313 After Hours: 260-599-8345 Email: groundwatertech@flintandwalling.com 95 N Oak Street Kendallville, IN 46755 USA
Please note that the guides below are general in nature. Please refer to your instruction manual for specific information regarding your product.
4″ Submersible Pump
Possible Cause
Corrective Action
Incorrect voltage at motor
Check for correct wire size. Replace undersize wire. Check line voltage, contact power company if voltage is incorrect
Defective fuse box or incorrect fuses
Inspect fuse box wiring and correct. Install the proper fuses
Defective pressure switch
Replace pressure switch or clean contacts
Control box malfunction
See control box checking and repairing procedures. Replace defective components
Defective drop cable insulation
Check drop cable insulation resistance. Pump must be pulled to replace defective cable
Motor malfunction
Check motor winding resistance. Pump must be pulled to replace defective motor
Pump malfunction
If all above checks are good, then pump is probably bound. Pump must be pulled. Check for sand or pump shaft misalignment. Correct well condition if sand is the problem
Possible Cause
Corrective Action
No power to start motor
Check voltage at line side of fuse box. Contact power company if no power is reaching box. Check voltage at load side of fuse box and at other control devices in circuit. Make necessary corrections
Defective drop cable or motor
Check motor winding resistance. Pump must be pulled to replace defective cable or motor
Possible Cause
Corrective Action
Air locked pump
Normal delivery may resume if water pump is started and stopped at one minute intervals
Gas or air in well water
Connect hose to service valve. Run water thru hose submerged in water in clear jar. Observe for air bubbles from hose outlet. If tank is standard type, the air volume control may be defective – replace; otherwise, have well checked for proper water level as pump may be drawing air. Lower pump and/or correct well condition
Low water level in well or pumping too much from well
Throttle pump with gate valve. Lower pump setting if depth of well is adequate
Defective or improperly installed check valve
Pump must be raised to replace or reinstall correctly
Leak in drop pipe damaged section
Raise pump, check pipe for leak and replace
Pump inlet screen blocked
Raise pump and clean screen. Verify that well is clean. Reset pump at less depth if possible
Worn pump
Pull pump and replace damaged components
Broken pump shaft or motor shaft or worn coupling
Pull pump, inspect shafts and coupling for damage. Replace defective components
Possible Cause
Corrective Action
Pressure switch
Readjust switch to lower shut off pressure setting, clean contacts or replace switch
Low water level
Throttle pump outlet at gate valve or readjust pressure switch to lower shutoff pressure setting
Leak in drop pipe or worn pump
Throttle pump output at gate valve or readjust pressure switch to lower shut off pressure setting. If pump does not shut off, pump must be raised and defect repaired
Possible Cause
Corrective Action
Pressure switch
Readjust switch to wider operating pressure limits; replace defective switch
Air volume in tank incorrect
Check pressure in tank. Set at 2 lbs. below turn on pressure of the pressure switch. i.e. 30/50 pressure switch should have tank pressure of 28 lbs.
Check valve defect or leak in drop pipe
Throttle pump output at gate valve. If pump does not shut off, pump must be raised and defect repaired
VFD System Trip Code Troubleshooting
Possible Cause
Corrective Action
Shorted motor cables
Check motor wires and drop cable for shorts or bad connections
Shorted motor
Replace motor
Damaged wire insulation
Check drop cable for insulation damage
Internal hardware short
If motor is disconnected and the fault is present when reset, replace drive
Possible Cause
Corrective Action
Motor/pump misaligned
Verify pump is mounted flush on motor mounting flange.
Bound pump
Check for debris in pump
Possible Cause
Corrective Action
Drive set for Switch control, but a transducer signal was detected.
Change drive control choice from Switch to Transducer in Control Choice menu
Possible Cause
Corrective Action
Drive has detected a short circuit between S1 & S2 terminals
Internal short of transducer. Replace transducer.
Switch is hooked up between S1 & S2
Replace switch with transducer.
Possible Cause
Corrective Action
Transducer lead not connected properly to transducer (or cut)
Check transducer lead connection and/or replace transducer lead wire.
Loose connection on terminals S1 & S2
Check transducer lead connection at drive terminals S1 & S2
Transducer lead wire backwards at S1 & S2 terminals
Switch transducer leads at S1 & S2
Transducer failed as an open circuit
Replace transducer
Possible Cause
Corrective Action
Pump running against a closed discharge.
Make sure that there is not a valve closed or obstruction between the pump and pressure switch
Damaged or clogged pressure switch
Check continuity across switch contacts without wire connected and replace and/or clean pressure port.
Deadhead sensitivity incorrect
Adjust deadhead sensitivity in Underload Protection menu
Possible Cause
Corrective Action
Pump running against a closed discharge.
Make sure that there is not a valve closed or obstruction between the pump and pressure transducer
Deadhead sensitivity incorrect
Adjust deadhead sensitivity in Underload Protection menu
Clogged pressure transducer
Check transducer for pressure port and clean
Damaged or inoperative transducer
Replace transducer
Possible Cause
Corrective Action
Over pumped/dry well
Wait for well to recover and automatic restart timer to time out
Blocked pump screen
Clear pump screen
Broken pump shaft
Replace pump shaft (or pump)
Worn pump
Replace pump
Possible Cause
Corrective Action
Low line voltage
Check line voltage. Report low voltage to the power company
Power was removed from Drive
Check voltage is present on all input lines & connections secure
Possible Cause
Corrective Action
Loose connection
Check connections on drive motor terminals for leg specified
Defective splice
Check all splice connections on drop cable for leg specified
Defective cable
Check continuity of drop cable for leg specified
Open motor winding
Replace motor
Possible Cause
Corrective Action
Check that the ambient temperature is not above 125°F
Excessive heating of Drive
Check for obstructed or inoperable fan
Check for blocked vents
Possible Cause
Corrective Action
Drive has been running without going into standby mode for set time
Check for broken or leaking pipe and repair as necessary
Application calls for long run time
Increase broken pipe run time in Advanced Feature menu
Turn off Broke Pipe protection in Advanced Feature menu
Possible Cause
Corrective Action
Contacts closed on “Alarm In” terminals
Check condition of switch wired into “Alarm In” terminals
VFD System Troubleshooting
Possible Cause
Corrective Action
Motor/Pump is running backwards.
Switch two of the three wires leading from the controller to the 3-phase motor.
Pump capacity cannot supply the demand.
Use pump with higher flow rating (if head requirement is still satisfied).
Temperature in the controller is too high. If the controller’s heat exchanger becomes too hot, the controller will reduce the output frequency to the motor to lower the power consumption.
Make sure there is at least 4 inches of room around the controller for movement of air. Avoid direct sunlight. Reduce ambient temperature below 104°F (40°C). Increase input voltage if below 230 VAC.
Pump capacity cannot supply the demand.
Use pump with higher flow rating (if head requirement is still satisfied).
Possible Cause
Corrective Action
Waterlogged tank.
Check tank for bladder damage. Replace if necessary.
Reset the tank pre-charge pressure (should be 70% of pressure switch/transducer setting).
Pressure tank is too small for flow rating of the pump.
Use larger tank (4 gal. tank minimum).
Possible Cause
Corrective Action
Bad pressure switch
Check continuity across pressure switch terminals and replace if necessary
Loose pressure switch wire connection or broken wire
Check pressure switch wire connections on display board and at pressure switch. Check wire for continuity.
Drive is in switch control mode and transducer is hooked up backwards.
Check to ensure transducer brown lead is connected to S1 and blue lead is connected to S2 terminals. Change control mode from switch to transducer.
Possible Cause
Corrective Action
Leak in the household or outdoor plumbing.
Check for leaky faucets, valves and/or pipe fittings and repair.
Leak in the pitless adapter.
Re-seat the pitless adapter. Replace seal as needed.
CJ101, CJ103 Centrifugal Pump Troubleshooting
Possible Cause
Corrective Action
Pump not primed
Prime unit
Total head too high
Shorten suction lift and/or discharge head
Suction head higher than pump designed for
Lower pump inlet
Impeller clogged
Clean
Incorrect rotation
Refer to wiring information
Leak in suction line
Repair or replace
Inadequate foot valve
Make needed adjustments
Impeller damaged
Replace
Foot valve or suction line not submerged deep enough in water
Submerge lower in water
Insufficient inlet pressure or suction head
Increase inlet pressure by adding more fluid to fluid source
Wrong size piping
Make needed adjustments
Casing gasket leaking
Replace gasket
Suction or discharge line valves closed
Open
Possible Cause
Corrective Action
Air leak in suction line
Repair
Suction head too high
Lower pump inlet
Insufficient inlet pressure or suction head
Increase inlet pressure by adding more fluid to fluid source
Clogged foot valve or strainer
Clean or replace
Possible Cause
Corrective Action
Mounting plate or foundation not rigid enough
Reinforce
Foreign material in pump
Clean
Damaged impeller
Replace
Cavitation present
Check suction line for proper size and be certain valve is open. Remove excessive loops in suction line
Worn motor bearings
Replace
Bent impeller shaft
Replace
Possible Cause
Corrective Action
Improperly wired
Refer to wiring diagram
Blown fuse or open circuit breaker
Replace fuse or close circuit breaker
Loose or broken wiring
Tighten connections and replace broken wiring
Impeller clogged
Clean
Motor shorted out
Replace
Possible Cause
Corrective Action
Damaged or worn mechanical seal
Replace
Corrosion due to character of liquid pumped
Discontinue pumping liquid and consult factory
C22000 Centrifugal Pump Troubleshooting
Possible Cause
Corrective Action
Incorrect rotation
Refer to wiring diagram
Insufficient inlet pressure or suction head (NPSH Required)
Increase inlet pressure by adding more fluid to fluid source. (See Spec’s for minimum NPSH Required)
Total head too high
Lower discharge head
Leak in suction line
Repair or replace
Impeller clogged or damaged
Clean or replace
Wrong size piping
Make needed adjustments
Casing gasket leaking
Replace gasket
Suction or discharge line valves closed
Open
Mechanical seal leaking
Replace
Possible Cause
Corrective Action
Insufficient inlet pressure or suction head (NPSH Required)
Increase inlet pressure by adding more fluid to fluid source. (See Spec’s for minimum NPSH Required)
Clogged strainer
Clean or replace
Possible Cause
Corrective Action
Mounting plate or foundation not rigid enough
Reinforce
Foreign material in pump
Clean
Damaged impeller
Replace
Cavitation present
Check suction line for proper size and be sure valve is open. Remove excessive loops in suction line. (See Spec’s for minimum NPSH Required)
Possible Cause
Corrective Action
Damaged or worn mechanical seal
Replace
Corrosion due to character of liquid pumped
Discontinue pumping liquid and consult factory
Possible Cause
Corrective Action
Improperly wired
Refer to wiring diagram
Blown fuse or open circuit breaker
Replace fuse or close circuit breaker
Loose or broken wiring
Tighten connections and replace broken wiring
Impeller clogged
Clean
Motor shorted out
Replace
Possible Cause
Corrective Action
Various
Consult qualified electrician
Overloading motor. Too much water delivery
Restrict outlet by closing down valve in discharge line
Liquid heavier and more viscous than water
Consult factory
Seal binding
Replace
Rotor binding
Repair or replace
Voltage and frequency lower than rating
Reconnect to rated voltage and frequency
Defects in motor
Repair or replace
Possible Cause
Corrective Action
Cavitation caused by insufficient inlet pressure or suction head (NPSH Required)
Increase inlet pressure by adding a higher level of fluid to source or increasing inlet pressure. (See Spec’s for minimum NPSH Required)
Pump Won’t Start or Run at Full Speed
Possible Cause
Corrective Action
Manual or solenoid valves plumbed into system restricting flow
a. Check all valves on pump inlet and discharge sides of system to be sure they are opened properly to allow flow to and from the pumpb. Bleed trapped air in pump which keeps water from reaching the pump. (Normally due to closed valve in discharge plumbing)
In-line filter restricting flow
Check all in-line filters to be sure they are not plugged or restricted
Low line voltage
See low line voltage corrective action (above)
Inadequate water supply to booster pump
Check pressure on inlet side of booster to be sure positive pressure is maintained to the booster pump
Undersized piping
Replace undersized piping
Leak on inlet side of system
Make sure connections are tight. Repair leaks as necessary
Inadequate, defective or plugged foot valve and/or strainer
Clean, repair or replace as needed
Worn or defective pump parts or pump
Replace worn parts or entire plugged impeller. Clean parts if necessary.
Suction lift too great
Pump should be operated under
flooded suction only
Pump not primed
Prime pump – Make certain inlet pipe is drawn up tight and pump and pipe are full of water
Incorrect rotation, motor running backwards
Reverse motor rotation can occur on three phase units. To correct, interchange any two incoming power leads.
Possible Cause
Corrective Action
Pump not secured to firm foundation
Secure properly
Piping not supported
Make necessary adjustments
Restricted inlet line
Clean or correct
Cavitation (noise like marbles in pump)
a. Reduce speed on direct driveb. Increase inlet pipe sizec. Too viscous (material being pumped too thick
Worn motor bearings
Replace bearings or motor
Possible Cause
Corrective Action
Worn mechanical seal (leaks at shaft)
Replace shaft (rotary) seal
Worn o-ring seals
Replace o-ring seals, located inside both ends of the stainless steel shell
City Pressure Booster
Possible Cause
Corrective Action
No power supply
Connect the electricity supply.
Incorrect voltage
Pump is 115 Volt only. It will not start with 230V supply.
Incorrectly plumbed
Confirm FIG 1 installation in the instructions is correct. Confirm ball valves #1 and #2 are open in suction and discharge. Confirm ball valve #3 is closed on bypass.
Blocked inlet
Check if pump suction inlet screen is blocked. See fig 5 in the instructions.
Insufficient water supply
Insure water source is providing sufficient water.
Possible Cause
Corrective Action
Pipe leaking
Insure all threads have 3 wraps of Teflon tape + hand tight + 1/2 turn with wrench.
Tank pressure is low
See FIG 3 in the instructions to check and add air pressure to the tank.
Air in the system
Insure all threads have 3 wraps of teflon tape + hand tight + 1/2 turn with wrench. Re-prime unit.
Possible Cause
Corrective Action
Blocked check valve
See fig 4 in the instructions. Confirm check valve is free of debris and functions freely.
SPJ Irrigation Pump
Possible Cause
Corrective Action
Casing not initially filled with water
Fill pump casing
Total head too high
Shorten suction lift and/or change head
Suction lift too high, or too long
Lower suction lift, install foot valve and prime, or shorten length of suction line
Impeller plugged
Clean
Hole or air leak in suction line
Repair or replace; do not use Teflon tape; use pipe sealing compound
Foot valve too small
Match foot valve to piping or install one size larger foot valve.
Impeller damaged
Replace
Foot valve or suction line not submerged deep enough in water
Submerge lower in water
Insufficient inlet pressure or suction head
Increase inlet pressure by adding more water to tank or increasing back pressure
Suction piping too small
Increase to pump inlet size or one size larger
Motor wired incorrectly
Check wiring diagram
Casing gasket leaking
Replace
Suction or discharge line valves closed
Open
Possible Cause
Corrective Action
No priming water in casing
Fill pump casing
Leak in suction line
Repair or replace
Discharge line is closed and priming air has nowhere to go
Open ball valve
Suction line (or valve) is closed
Open
Foot valve is leaking
Replace foot valve
Suction screen clogged
Clean or replace
Possible Cause
Corrective Action
Air leak in suction line
Repair or replace
Suction lift too high
Lower suction lift, install foot valve and prime
Insufficient inlet pressure or suction head
Increase inlet pressure by adding more water to tank or increasing back pressure
Clogged foot valve or strainer
Unclog
Possible Cause
Corrective Action
Mounting plate or foundation not rigid enough
Reinforce
Foreign material in pump
Disassemble pump and clean
Impeller damaged
Replace
Worn motor bearings
Replace
Possible Cause
Corrective Action
Improperly wired
Check wiring diagram on motor
Blown fuse or open circuit breaker
Replace fuse or close circuit breaker
Loose or broken wiring
Tighten connections, replace broken wiring
Stone or foreign object lodged in impeller
Disassemble pump and remove foreign object
Motor shorted out
Replace
Thermal overload has opened circuit
Allow unit to cool, restart after reason for overload has been determined
Possible Cause
Corrective Action
Worn mechanical seal
Replace (see Rotary Seal Replacement)
Shallow Well Jet Pump
Possible Cause
Corrective Action
Casing not initially filled with water
Fill pump casing
Suction lift too high, or too long
Move pump closer to water source
Hole or air leak in suction line
Repair or replace. Use pipe tape and pipe sealing compound
Foot valve too small
Match foot valve to piping or install one size larger foot valve.
Foot valve or suction line not submerged deep enough in water
Submerge lower in water
Motor wired incorrectly
Check wiring diagram
Casing gasket leaking
Replace
Suction or discharge line valves closed
Open
Possible Cause
Corrective Action
No priming water in casing
Fill pump casing
Leak in suction line
Repair or replace
Discharge line is closed and priming air has nowhere to go
Open ball valve
Suction line (or valve) is closed
Open
Foot valve is leaking
Replace foot valve
Suction screen clogged
Clean or replace
Possible Cause
Corrective Action
Air leak in suction line
Repair or replace
Suction lift too high
Lower suction lift, install foot valve and prime
Insufficient inlet pressure or suction head
Increase inlet pressure by adding more water to tank or increasing back pressure
Clogged foot valve or strainer
Unclog
Possible Cause
Corrective Action
Mounting plate or foundation not rigid enough
Reinforce
Foreign material in pump
Disassemble pump and clean
Impeller damaged
Replace
Worn motor bearings
Replace
Possible Cause
Corrective Action
Improperly wired
Check wiring diagram on motor
Blown fuse or open circuit breaker
Replace fuse or close circuit breaker
Loose or broken wiring
Tighten connections, replace broken wiring
Stone or foreign object lodged in impeller
Disassemble pump and remove foreign object
Motor shorted out
Replace
Thermal overload has opened circuit
Allow unit to cool, restart after reason for overload has been determined
Convertible Deepwell Jet Pump
Possible Cause
Corrective Action
Casing not initially filled with water
Fill pump casing
Suction lift too high, or too long
Move pump closer to water source
Hole or air leak in suction line
Repair or replace. Use pipe tape and pipe sealing compound
Foot valve too small
Match foot valve to piping or install one size larger foot valve
Foot valve or suction line not submerged deep enough in water
Submerge lower in water
Motor wired incorrectly
Check wiring diagram
Casing gasket leaking
Replace
Suction or discharge line valves closed
Open
Possible Cause
Corrective Action
No priming water in casing
Fill pump casing
Leak in suction line
Repair or replace
Discharge line is closed and priming air has nowhere to go
Open ball valve
Suction line (or valve) is closed
Open
Foot valve is leaking
Replace foot valve
Suction screen clogged
Clean or replace
Possible Cause
Corrective Action
Air leak in suction line
Repair or replace
Suction lift too high
Lower suction lift, install foot valve and prime
Insufficient inlet pressure or suction head
Increase inlet pressure by adding more water to tank or increasing back pressure
Clogged foot valve or strainer
Unclog
Possible Cause
Corrective Action
Mounting plate or foundation not rigid enough
Reinforce
Foreign material in pump
Disassemble pump and clean
Impeller damaged
Replace
Worn motor bearings
Replace
Possible Cause
Corrective Action
Improperly wired
Check wiring diagram on motor
Blown fuse or open circuit breaker
Replace fuse or close circuit breaker
Loose or broken wiring
Tighten connections, replace broken wiring
Stone or foreign object lodged in impeller
Disassemble pump and remove foreign object
Motor shorted out
Replace
Thermal overload has opened circuit
Allow unit to cool, restart after reason for overload has been determined
Fountain Pond Pump
Possible Cause
Corrective Action
Circuit breaker tripped
Reset circuit breaker
Low Voltage
Verify voltage
GFI Tripped
Reset GFI
Excessive Cable Length
Verify acceptable maximum cable length
Timer/clock not set
Set clock to local time and timers for desired cycle. See Section on Setting Timers
Possible Cause
Corrective Action
Blocked screen or nozzle, missing or damaged o-ring, or incorrectly installed nozzle
Disconnect power. Clean screen and/or nozzle. Check that o-ring is undamaged and seated in groove. Check that nozzle is installed properly (nozzles are marked “This side up”). Check depth of pond. If less than 5 feet deep, move to deeper section. Restart unit.
Possible Cause
Corrective Action
Electrical storm can trip GFI
Reset GFI
Short in system
Disconnect power and check cord for damage. If cord is damaged contact customer service help line at 1-800-742-5044.
Defective power cable
Disconnect power and check cord for damage. If cord is damaged contact customer service help line at 1-800-742-5044.
Possible Cause
Corrective Action
Anchor rope(s) loose
Check anchor rope(s) and re-attach if necessary
Water Conditioner
Possible Cause
Corrective Action
Transformer unplugged
Connect power
No electric power at outlet
Repair outlet or use working outlet
Defective transformer
Replace transformer
Defective PC board
Replace PC board
Possible Cause
Corrective Action
Switched outlet
Use uninterrupted outlet
Power outage
Reset time of day
Defective PC board
Replace PC board
Possible Cause
Corrective Action
Bypass valve in bypass position
Put bypass valve in service position
Meter connection disconnected
Connect meter to PC board
Restricted/stalled meter turbine
Remove meter and check for rotation or foreign material
Defective meter
Replace meter
Defective PC board
Replace PC board
Possible Cause
Corrective Action
Power outages
Reset control valve to correct time of day
Time of day not set correctly
Reset to correct time of day (A.M./P.M.)
Time of regeneration incorrect
Reset regeneration time (A.M./P.M.)
Control valve set at “on 0” (immediate regeneration)
Check control valve set-up procedure regeneration time option
Control Valve set at NORMAL + “on 0”
Check control valve set-up procedure regeneration time option
Possible Cause
Corrective Action
1001 Error Code – Unable to recognize start of regeneration
1002 Error Code – Unexpected stall
1003 Error Code – Motor ran too long, timed out trying to reach next cycle position
1004 Error Code – Motor ran too long, timed out trying to reach home positionIf other Error Codes display, contact the factory
1. Correct error condition
2. Press “NEXT” and “REGEN” simultaneously for three seconds
Control valve has just been serviced
Press “NEXT” and “REGEN” for 3 seconds, or unplug power source jack (black wire) and plug back in to reset control valve
Foreign matter is lodged in control valve
Check piston and spacer stack assembly for foreign matter
High drive forces on piston
Replace piston(s) and spacer stack assembly
Control valve piston not in home position
Press “NEXT” and “REGEN” for 3 seconds or unplug power source jack (black wire) and plug back in to reset control valve
Motor not inserted fully to engage pinion, motor wires broken or disconnected, motor failure
Check motor and wiring. Replace motor if necessary
Drive gear label dirty or damaged, missing or broken gear
Clean drive gear(s)
Drive bracket incorrectly aligned to back plate
Re-seat drive bracket properly
PC board is damaged or defective
Replace PC board
PC board incorrectly aligned to drive bracket
Ensure PC board is correctly snapped on to drive bracket
Possible Cause
Corrective Action
Motor not operating
Replace motor
No electric power at outlet
Repair outlet or use working outlet
Defective transformer
Replace transformer
Defective PC board
Replace PC board
Broken drive gear or drive cap assembly
Replace piston kit assembly
Broken piston retainer
Replace piston kit assembly
Broken main or regenerant piston
Replace piston kit assembly
Possible Cause
Corrective Action
Transformer unplugged
Connect transformer
No electric power at outlet
Repair outlet or use working outlet
Broken drive gear or drive cap assembly
Replace piston kit assembly
Defective PC board
Replace PC board
Possible Cause
Corrective Action
Bypass valve in bypass position
Put control valve in service position
Meter connection disconnected
Connect meter to PC board
Restricted/stalled meter turbine
Remove meter and check for rotation or foreign material
Defective motor
Replace meter
Defective PC board
Replace PC board
Set-up error
Check control valve set-up procedure
Possible Cause
Corrective Action
Power has been out more than two hours
Reset the time of day
The transformer was unplugged and then plugged back into the wall outlet
Reset the time of day
The transformer plug was unplugged and then plugged back into the board
Reset the time of day
The “NEXT” and “REGEN” buttons were pressed to reset the valve